It was stock timing, after putting it together my self and riding like a fool for 3000 miles and surviving on the dyno for two days and coming apart at 7000rpm im ok, best time of my life. The static compression being high may not have caused this, there is no signs of detonation in the other 2 cylinders, they look great. This is probably mechanical as the valves snapped off and beat the piston up, it didnt melt, i had the exhaust valves too tight i can almost guarantee it. Even though i failed, I learned and im fixing to put together a very strong motor thats gonna survive the dyno and be a hoot to pilot.